after error the red led blink few time and after that start blink green ones and head move in +x and +y at the same time cca 200mm
i dont think that content log give will be helpfull buet here is it:
Code: Select all
{"r":{"fv":0.970,"fb":438.02,"hp":1,"hv":8,"id":"3X3566-KYP","msg":"SYSTEM READY"},"f":[1,0,0,6925]}
==> {"gc":"G0 X113.246 Y120.577"}
tinyg [mm] ok>
qr:32, qi:1, qo:1
{"r":{},"f":[1,0,30,131]}
PutPartDown_m(): Probing placement Z
Probing Z, timeout value: 10
### {"zsn",0} ignored, cnc is in error state
### {"zsx",1} ignored, cnc is in error state
### {"zzb",0} ignored, cnc is in error state
### {"gc":"G28.4 Z0"} ignored, cnc is in error state
### {"zsn",3} ignored, cnc is in error state
### {"zsx",2} ignored, cnc is in error state
### {"zzb",2} ignored, cnc is in error state
{"sr":{"posx":0.000,"posy":0.000,"posz":0.000,"posa":0.000,"feed":0.00,"vel":1.39,"unit":1,"coor":0,"dist":0,"frmo":1,"stat":5}}
{"qr":31,"qi":1,"qo":0}
{"sr":{"posx":9.191,"posy":9.786,"vel":12072.89}}
{"sr":{"posx":53.894,"posy":57.383,"vel":24139.54}}
{"sr":{"posx":101.824,"posy":108.415,"vel":14241.25}}
{"sr":{"posx":113.239,"posy":120.569,"vel":102.71}}
{"sr":{"posx":113.246,"posy":120.577,"vel":0.00,"stat":3}}
ReadyEvent stat
{"qr":32,"qi":0,"qo":1}
###{"gc":"M05"} discarded, error state on
CNC_XY_m, x: 112.746, y: 120.077
### Cnc in error state, ignored
CNC_XY_m, x: 113.746, y: 121.077
### Cnc in error state, ignored
VacuumOff()
###{"gc":"M09"} discarded, error state on
Code: Select all
==> {"gc":"G0 X94.111 Y106.393 A359.8556"}
{"r":{},"f":[1,0,39,140]}
{"sr":{"posx":194.954,"posy":191.334,"posa":270.000,"vel":2.16,"stat":5}}
{"qr":31,"qi":1,"qo":0}
{"sr":{"posx":185.539,"posy":183.404,"posa":278.389,"vel":12180.25}}
{"sr":{"posx":153.553,"posy":156.462,"posa":306.890,"vel":15822.27}}
{"r":{"fv":0.970,"fb":438.02,"hp":1,"hv":8,"id":"3X3566-KYP","msg":"SYSTEM READY"},"f":[1,0,0,6925]}
==> {"gc":"G0 X94.511 Y106.793"}
tinyg [mm] ok>
qr:32, qi:1, qo:1
PlacePart_m(): Part down, Z28.483
{"r":{},"f":[1,0,29,109]}
{"sr":{"posx":0.000,"posy":0.000,"posz":0.000,"posa":0.000,"feed":0.00,"vel":1.82,"unit":1,"coor":0,"dist":0,"frmo":1,"stat":5}}
{"qr":31,"qi":1,"qo":0}
{"sr":{"posx":7.764,"posy":8.773,"vel":9941.33}}
{"sr":{"posx":35.235,"posy":39.814,"vel":13353.70}}
{"sr":{"posx":64.376,"posy":72.741}}
{"sr":{"posx":90.160,"posy":101.876,"vel":7682.08}}
{"qr":32,"qi":0,"qo":1}
{"sr":{"posx":94.511,"posy":106.793,"vel":0.00,"stat":3}}
ReadyEvent stat
###{"gc":"M05"} discarded, error state on
CNC_XY_m, x: 94.011, y: 106.293
### Cnc in error state, ignored
CNC_XY_m, x: 95.011, y: 107.293
### Cnc in error state, ignored
VacuumOff()
###{"gc":"M09"} discarded, error state on
{"r":{"fv":0.970,"fb":438.02,"hp":1,"hv":8,"id":"3X3566-KYP","msg":"SYSTEM READY"},"f":[1,0,0,6925]}
tinyg [mm] ok>
qr:32, qi:1, qo:1
Code: Select all
==> {"gc":"G0 X96.375 Y114.023"} here blue
{"r":{"fv":0.970,"fb":438.02,"hp":1,"hv":8,"id":"3X3566-KYP","msg":"SYSTEM READY"},"f":[1,0,0,6925]}
tinyg [mm] ok>
qr:32, qi:1, qo:1
{"r":{"err":"{\""},"f":[1,108,3,5325]}
ReadyEvent r
{"sr":{"posx":0.000,"posy":0.000,"posz":0.000,"posa":0.000,"feed":0.00,"vel":0.00,"unit":1,"coor":0,"dist":0,"frmo":1,"stat":1}}
PlacePart_m(): Part down, Z28.483
###{"gc":"M05"} discarded, error state on
CNC_XY_m, x: -0.5, y: -0.5
### Cnc in error state, ignored
CNC_XY_m, x: 0.5, y: 0.5
### Cnc in error state, ignored
VacuumOff()
###{"gc":"M09"} discarded, error state on
you suggestion is to move by rewire everything? it works until last week and from that time i added only camera, bcs old one stopped worked.
im thinking if it can have overtemperature origin.